NNfC monthly admin committee meeting Dry Etch and Thin films & Process Integration Jan 6th, 2015 Dry Etch– Tool status Update Dec 2014 • RIE – AMC 2014 – Etch rate optimization post AMC • Etch rates were same as before except SiO2 , SiO2 etch rate decreased by 20nm/min. – Installation of Thermocouple for RIE-Cl has to be done. – DC bias interlock is installed in RIE-Cl (Max 500V). Al2O3 and ITO recipes are optimized accordingly. (No etch rate and profile variation) • PECVD – AMC 2014 – Post AMC deposition rates were checked- Same results as before with good uniformity. – Issue with Wafer Lift Bellow Assembly- Wafer transfer is done in manual mode. Spare part acquired and need to be installed. – SiO2 High deposition rate recipe optimization in process. Tool issues – Nov-Dec 2014. • eBeam deposition: Issue with GOLD deposition … seeing “gold balls” on surface of the films on the order od 1-2 microns! This is could be the potential cause of the failure of the RFMEMS switch for MSRIT project. Several other users have seen the same issue. Meeting organized to collect all the available data and trouble-shoot the problem. Problem seen since mid-Nov. • Sputter tools: Sputter2 down since early-Dec due to a faulty controller on the Throttle valve. Problem identified as the Norcal-valve controller— Quote received from Singapore~US$2.5k Need a strong push to Tecport for providing the part as part of the remaining spares money ~ US$38k. Sputter one is up – Need to purchase Al/Cr targets. Quotations received. P.O. requested. 3 Tool issues • DRIE: TOOL DOWN due to Arching in the Busbar area near the ICP Coil. Same problem seen in June 2014. SPTS had serviced the machine and cleaned the “blackened” contacts Tool was operating under reduced power conditions to avoid such arching Busbar parts were ordered in October, but the process has been slow due to strike and holidays/ICEE conference. Need to accelerate the Annual maintenance schedule and change the “damaged” busbar parts. Plan to get operational again in the next couple of weeks … provided all the “ducks” line up and the planets are aligned 4 Equipment Utilization Chart- Nov1st-Dec15th, 2014 600 500 Total hrs 400 300 200 100 0 RFAnelvaEquip Sputteri1- non ng- office office hrs hrs Therma Therma l l Evapor Evapor atoratornon office office hrs hrs 180 540 180 540 pecvdpecvdnon office office hrs hrs DrieDrienon office office hrs hrs rie flrie flnon office office hrs hrs rie clrie clnon office office hrs hrs sputtersputter 1- 1- non office office hrs hrs sputtersputter 2- 2 - non office office hrs hrs E-beam E-beam evptrevptrnonoffice office hrs hrs Total 180 540 180 540 180 540 180 540 180 540 180 540 180 540 Unavailable 81 333 81 333 81 340 81 340 80 340 80 340 80 340 0 180 0 180 Downtime 15 18 0 0 0 0 7 0 0 0 100 200 0 0 0 0 0 0 Not Used 28 184 49 193 43 188 44 176 9 129 0 0 8 168 84 360 16 360 Used 56 5 50 14 56 12 48 24 91 71 0 0 92 32 96 0 164 0 200 Equipment Utilization Chart- Last four months of 2014 PECVD 180 DRIE RIE-F RIE-Cl Sputter Coater1 Sputter Coater2 E-beam Evaporator Anelva Thermal Sputter Evap. 160 Total hrs 140 120 100 80 60 40 20 0 SepOct Total No De v c SepOct No De v c SepOct No De v c SepOct No De v c SepOct No De v c SepOct No De v c SepOct No De v c SepOct No De v c SepOct No De v c 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 Unavailable 0 0 0 81 0 0 0 81 0 0 0 81 0 0 0 81 0 0 0 80 0 0 0 80 0 0 0 80 0 0 0 0 0 0 0 0 Downtime 0 0 52 15 54 0 0 0 0 0 27 0 12 0 28 7 16 0 0 0 0 0 16 10 0 0 0 0 0 0 0 0 0 0 0 0 Not Used 78 13 80 28 63 10 13 49 11 14 88 43 11 15 99 44 29 22 27 9 11 80 11 0 16 20 52 8 24 48 68 96 36 40 40 16 Used 10 48 48 56 63 78 47 50 70 34 65 56 56 28 53 48 13 15 15 91 62 10 54 0 16 16 12 92 15 13 11 84 14 14 14 16 MTRDC project progress • Unit process development started in Aug. – Key challenges in eChannel RIE, Au-seed layer, gold plating, wafer bonding and dicing. • Prasiddhi mask ordered to start structural learning. Sadanand Deshpande, NNFC 7