Equipment Utilization Chart- February 2014 600 500 Total hrs 400 300 200 100 0 Total pecvdpecvdnon office office hrs hrs DrieDrienon office office hrs hrs rie flrie flnon office office hrs hrs rie clrie clnon office office hrs hrs sputte sputte r 1r 1non office office hrs hrs 180 540 180 540 180 540 180 540 180 540 sputte sputte r2r 2non office office hrs hrs EEbeam beam evptrevptrnonoffice office hrs hrs 180 540 180 540 CPD CPD non office office hrs hrs RFAnelvaEquip Sputte1- non ring- office office hrs hrs Therm Therm al al Evapor Evapor atoratornon office office hrs hrs 180 540 180 540 180 540 Unavailable 0 180 0 180 0 180 0 180 0 180 0 180 0 180 0 180 0 180 0 180 Downtime 0 0 2 0 0 0 0 0 0 0 0 0 16 12 35 22 0 0 0 0 0 196 Not Used 110 358 146 356 123 350 154 358 Used 70 32 57 26 2 4 10 2 180 164 128 336 72 308 114 336 28 360 36 352 52 92 31 152 144 24 40 2 0 8 Equipment Utilization Chart- Comparison 200 Sputter Coater1 Sputter E-beam Coater2 Evaporator Anelva Sputter Thermal Evap. No De Fe Jan v c b No De Fe Jan v c b No De Fe Jan v c b 18 18 18 18 18 18 18 18 18 18 18 18 0 18 18 18 18 0 40 0 0 0 45 0 0 0 0 0 0 PECVD DRIE RIE-Fl No De Fe Jan v c b No De Fe Jan v c b No De Fe Jan v c b No De Fe Jan v c b No De Fe Jan v c b No De Fe Jan v c b No De Fe Jan v c b 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 18 Unavailable 0 45 0 0 0 45 0 0 0 45 0 0 0 45 0 0 0 40 0 0 0 40 0 0 RIE-Cl 180 CPD 160 Total hrs 140 120 100 80 60 40 20 0 Total 0 0 0 0 Downtime 84 11 2 0 2 6 0 2 1 0 0 0 1 8 0 0 0 4 0 0 8 4 0 0 0 0 8 16 0 25 77 35 0 0 0 0 0 0 0 0 Not Used 82 21 10 11 14 90 15 14 13 88 14 12 16 10 14 15 0 0 4 0 14 11 12 12 84 64 68 72 93 78 85 11 64 96 60 28 84 10 76 36 Used 14 0 76 70 34 39 27 32 47 47 37 57 17 23 32 26 18 13 17 18 32 20 52 52 96 76 10 92 87 32 18 31 11 84 12 15 96 80 10 14 • DRIE Dry Etch– Tool status Update Feb 2014 – Load lock O-Ring changed . Ordered for new set. – Wafer transport issue – robot arm aligned. – Process: scallop smoothening trials in progress • • • • DRIE deep etches with S-Type wafer – scallops FGA anneals @1000DegC show no effect Scallop etch in RIE SEM imaging and process tuning in progress • RIE – Scallops smoothening • Combined process with DRIE. • using Anisotropic Si etch (RIE) smoothening scallops. • Result – scallop reduced to 145nm from 1.3 µm. • Trials for deeper etch and scallop size to be done. Reduced scallop – SiO2 plastering • Trench filling by PECVD SiO2 , followed by RIE SiO2 etch. • Work in progress for better conformal deposition. • PECVD vacuum leak in load lock –VAT valve to arrive tomorrow! Process is done in manual mode SiO2 plastering Technical Note