Update on LAV electronic M. Raggi, P. Valente G. Corradi, D. Tagnani, C. Paglia LNF electronic service LAV working group LNF 4/12/2009 1 Outline Signal flanges DB37 solution update HV system (distributors, connectors) Improving PMT divider performance 2 DB 37 flanges ECOVIDE projects 10 DB37 connectors Already asked for greater inter connector distance (30mm) 15 DB37 connectors Verified that 24 mm is enough with proper air side connector. Cabling difficulties to be evaluated in the vacuum side 3 DB37 connectors solution 20 mm Air Vacuum Vacuum Air Bring cables from the PMT to the back of the green connector on the right Minimize the discontinuity between the PMT and the electronic Reduce the number of connections in the cabling (less connectors) 4 HV system 5 HV connectors HV connector The distance between lateral pins and external connector crown is too small – Up 1.5 KV high voltage present – Inter pin distance max gap is only 0.5 KV – Asked ECOVIDE to improve the distance T (°C) I (nA) 25 80 45 5000 70 14000 60 2500 40000 50 550 30000 40 145 30 45 10000 80 35000 100 70000 0 75 3500 64 1200 48 204 39 566 80000 70000 60000 I(nA) 50000 20000 25 45 70 60 50 40 30 80 100 75 64 48 39 T(°C) 6 HV distributors o Can solve the 48-32 multiplicity problem removing 1 PCB as suggested by Riccardo o From a first by eye inspection of the boards: - Seems not feasible to change the HV range (500 V) due to insufficient isolation in PCB - Seems possible to switch off an entire board (16ch) to be studied o To change the specifications need to project a new PCB o No news concerning the connectors and cabling 7 Improving divider performance 8 PMT test station setup We built a LED based setup to test the tube performance – CAMAC driver to control LED light injection • 0-20V in input to LED 10-400 ns wdt in input to the LED – Automatic amplitude scan (0.1 V steps) at fixed width (10 ns) • LED pulses shorter wrt intrinsic LED time constant • Able to scan the entire QDC dynamics – Automatic start of Daq acquisition program • Readout of both QDC (dual range) and TDC • For each channel 2 different threshold are red out • Monitor of the LED emission current (new) – Still to implement automatic HV control 9 Test beam results For big signals a step in the ToT distribution is observed The step is due to the ringing overcoming the threshold thr ToT 10 Il ringing del segnale analogico L’oscillazione dipende dall’induttanza parassita degli ultimi 3 dinodi e l’anodo, causata dalla distanza tra partitore dinodo! The “shoulder” is due to a low value of the C3 capacitor. 11 Correct dynodes effect To correct the effect due dynodes d10 d11 d12 inductance the quenching coefficient must be increased: Cut the routes to d10, d11, d12 Insert one smd resistance on each route Ad a capacitor in parallel to C3 Ripregnare il PCB 12 Tube performance after dynodes quenching Same PMT @ 1250V L’oscillazione e’ sparita come previsto ma resta la spalla dovuta al fatto che i condensatori non sono ancora del valore esatto e risulta necessario inserire una resistenza anche sull’anodo. La correzione di questo effetto va ad intaccare l’RC del circuito quindi il tempo di salita del segnale risulta percio’ piu’ delicata Le conseguenze della spalla sulla misura di TOT sono di minor importanza ?? 13 Layout of new PCB for LAV PMTs was 220 V First dynode clamp (from 220V to 280V) Quenching of d10 d11 d12 and anode Quenching capacitor 14 Dynamic range result Original PMT (75 pC) Dynode quench(170 PC) Full modification Sensitivity region enhanced by factor near to 10 15 Residual problem Residual effect 3% of the 16 Conclusion The DB37 solution for the flanges is finalized − No problems for the ANTI-A1,A5 − Density on cables in the vacuum side to be evaluated for the ANTI-A6,A11 − Option with 2x10 connectors flanges feasible The new PCB production for the PMT seems mandatory – Improves the ToT by enlarging the sensitive region – Modify the present PCB requires too much work – Modify 10 components in the PCB is not feasible 17